The Philco 19B Cathedral from 1934 is a 6-tube superhet with
an RF amplifier stage. This example was Code 126. The Philco
19 is very
similar to the Philco 89, but has a Shadow Meter tuning aid.
The Philco 19, like the model 89, went through many changes and revisions during its life. It is difficult to find an accurate schematic for Code 126. The most accurate I was able to find was on Philco Radio, where the evolution of the model 19 is discussed. This information must be supplemented with schematics from Nostalgia Air under various model 19 variations and also under model 89. The schematic on Philcoradio.com is difficult to read, at least the part numbers. I was able to identify and write in the parts and part numbers using the Code 128 schematic on Nostalgia Air. The radio had seen minimal servicing in the past - most of the original parts were still in place. I decided to try to reverse all previous repairs to the extent possible. |
My antique radio restoration logs
This radio was purchased at the 2011 Charlotte AWA Radio Conference in the auction. The cabinet was in excellent original condition, as were the knobs and grille cloth. There was no evidence that the radio had been restored, although one filter capacitor was missing and there was tape on the leads to the Shadow Meter. I always avoid knowingly purchasing a radio that has been restored by a collector, as many take shortcuts such as removing the original Philco bakelite block capacitors and filters.
One original filter capacitor had been removed and replaced by a tubular electrolytic under the chassis
A couple of tubes had been replaced - the remainder were Philco branded and possibly original
The leads to the Shadow Meter had been cut, spliced back, and taped over. The pilot lamp behind the meter had been removed. This indicated that the meter was likely OPEN - later confirmed.
The shield base for the type 36 tube had been removed, and the tube socket was retained by only one rivet.
All the original Philco bakelite block capacitors and resistors were still in place.
It appeared that the dial cord had been replaced by a piece of heavy cotton cord.
My usual restoration procedure is to first make a complete survey of the condition of all components. The survey results guide my restoration strategy. If major and unique components are defective or missing and cannot be restored or replaced, I may elect to sell the radio rather than restore it. I always assume that all paper and electrolytic capacitors are leaky and thus should be replaced (I always "restuff" the original containers if possible). Any mica capacitors are assumed OK until testing proves otherwise.
At this point I made BEFORE photos of the chassis bottom. I use these photos to ensure that replacement parts and wiring are placed as close as possible to their original positions. Some radios are subject to problems (such as oscillation) if wiring is re-routed or lead dress is not the same as the original..
All tubes and tube shields were removed. The tuning capacitor and dial assembly was removed for cleaning and replacement of chassis grommets and dial cord. All non-original parts were then removed.
The top and sides of the chassis was cleaned with GoJo hand cleaner and 00 steel wool. Since this process may leave small steel wool fragments that can cause problems later, I follow up with a thorough vacuuming and go over everything with a small magnet and masking tape to pick up any stray fragments.
The remaining rivet was removed retaining the type 36 tube socket. Fortunately I had an original Philco shield base and tube shield in my Philco parts stock (although they were RUSTY!) The shield base and socket was then assembled using small 6-32 screws and very small 6-32 nuts.
The tuning capacitor grommets were replaced by GLg-Tuner grommets from Renovated Radio. The tuning capacitor was cleaned in an ultrasonic cleaner followed by soap, water, and toothbrushes. The bearings were then lubricated using distributor cam lubricant (which is similar to the original grease used). Before cleaning, the trimmer micas were removed in order to prevent damage. In order to get the trimmers back to approximately where they were originally set, I first note the position of the trimmer screw on the clock, then count the half turns (and fractions) from that position to fully tight. The mica sheets and trimmer hardware were also cleaned in the ultrasonic cleaner and then dried before reassembly. After reassembly, each trimmer is again turned to fully tight position, then backed off the appropriate number of half turns and fractions. This process will return the trimmers to close to their original positions (later fixed by a full alignment).
The combination power switch and band switch was removed from the radio and cleaned in an ultrasonic cleaner using water and dilute ammonia, followed be soap and water and a toothbrush. After this cleaning both the AC switch and band switch worked well.
The shadow meter coil was open. I used the service note information found on the Philco Repair Bench to repair this unit. The meter was disassembled and the coil removed. I first tried to probe the coil for continuity from the outside using an Exacto #11 knife blade, hoping that the break would be near the outside. In that case, it could be restored with minimal loss of turns. But no luck! So I was faced with rewinding the coil. The only suitable enamel wire I had in stock was very slightly larger in diameter than the original. I fabricated a suitable jig to hold the coil in the chuck of my Unimat lathe, as well as a holder for the supply spool of wire. The jig consisted of a piece very hard clock pivot wire about 1/16" diameter, plus a couple of wire nails to center the coil. A wrapping of #22 copper buss wire then secured the nails and wire. The wire was then chucked in the lathe. The lathe was run at its slowest speed. I left the belt guard open so I could stop the lathe instantly if needed. The wire had a tendency to wrap outside the form near the ends.
The wire did break twice during the rewind operation, but I was able to splice it back together in both cases. The resulting coil measured 956 ohms vs. 1100 ohms, likely due to using larger gauge wire. The meter was then assembled and tested using a variable power supply as suggested in the service note on the Philco Repair Bench. The meter did function as documented at 10 volts, and went back to almost zero width at zero volts in. When installed in the radio, the deflection on-tune was about 1/4" (to about 1/2" off tune). I guessed that this was due to the fact that I was only using a 20' piece of wire for an antenna (plus I am in a rural area). A longer antenna, or stronger signals, would have increased the AVC voltage and thus reduce the plate current and thus the width of the deflection on tune. But the meter did indeed function!
All original Philco bakelite block capacitors were removed from the radio, their contents removed, cases cleaned, and restuffed using modern film capacitors. The AVC filter capacitor block, with its two 110pf capacitors, was restuffed using 100pf dipped mica capacitors. One other bakelite block capacitor had a wire wound resistor inside in addition to a bypass capacitor. This resistor was reused.
All original dogbone and cast end resistors were within acceptable tolerances and were left in place.
The tone switch capacitor was removed, the insulator salvaged, the two capacitors replaced, and the case resealed using melted rosin left over from restoration of RCA superhet catacombs. This wax melts at low temperatures and will not damaged new components. Some collectors use tinted hot glue or even caulk for resealing components.
The metal cased bypass capacitor C7, with 5 capacitors inside, was restuffed using new film capacitors. I was able to salvage the original lead wires and reuse them. The capacitor consisted of two .09mfd, two .05mfd, and one .25mfd unit. It was restuffed with two .1mfd, two .047mfd, and one .22mfd film capacitor. The original insulator inside was retained and reused. The new parts were sealed using melted rosin.
One original filter capacitor (6mfd) had been removed, and a tubular replacement installed under the chassis. I had a similar dud in my used parts collection, and recycled the required cardboard insulator from another dud capacitor which was the same size. Both the original and replacement duds were restuffed using 10mfd/450 volt electrolytics. To restuff, the capacitors were chucked in my Unimat lathe and their cases scored about 1" from the bottom. The cuts were then completed using a hobby razor saw. The original contents were then removed and the capacitor case cleaned inside and out. The remaining original capacitor had a very soft aluminum threaded stud which was damaged during removal. This was drilled out and a 10-24 screw substituted, along with a ground lug for attaching the new filter capacitor. The negative lead of the new capacitor was routed though a small hole drilled into the hard rubber base and attached to the original ground lug.
The two 44 tubes were replaced by used/tested 39/44 tubes. The 42 tube was replaced.
The cabinet only needed a good vacuuming inside and then cleaning on the outside with GoJo and 00 steel wool, plus removal of the deteriorated chassis washers. The chassis washers were replaced using 7/8" x 3/8" washers from Renovated Radios (CW-4).
Once the radio chassis was reassembled and the tubes installed, power was brought up slowly using a variac. AC power consumption was monitored using a watt meter, and a DVM monitored the B+. The radio powered up and worked on both the broadcast and short wave bands. The radio was then aligned, although all adjustments were very close to correct.
The radio performs well, and has very good tone. Even the short wave band works. Perhaps due to the use of 10mfd filter capacitors instead of the original 6mfd, the B+ is higher than specification even with only 110 volts AC input! So this radio, like most others in my collection, will only be operated using my bucking transformer.